Installed FMIC last night. But hose on the charge pipe side blew off wasn't tight enough. Drove it back home super slow, popped it back on. Double checked it all seems good. But wasnt making any boost (maybe in limp mode). Cleared all codes, reflashed tune. Now I'm pulling 18 lbs instead of 21, car feels a little tired. With a new FMIC I was expecting 1-2 lb drop of boost denser air and of course more piping. But maybe the car is relearning? Idk spooked me good. Once car cools off I’ll wiggle the compressor on the turbo.
Little info on the car running a stratified tune basic bolt ons, pancake pipe, charge pipe, downpipe intake, 2012 gti of course.
Little info on the car running a stratified tune basic bolt ons, pancake pipe, charge pipe, downpipe intake, 2012 gti of course.
Last edited: